Work done on April 9:
* Dana wanted to go up line to get rail (for the new siding) and look for new timbers to replace the south AC switch stand timbers, but the diesel's batteries were dead. So the morning was spent charging them up.
* Zack and Bob G worked to jack up #9's old boiler to get the truck underneath out. Eventually that happened.
* Because the diesel was down, I fired up the Brookville (behind Coach 3 in the shop), got hooked up, and pushed it and Car 103 out to the mainline. Then we got the two flatcars hooked up and moved out of the way. Then all the stuff on track 7 got moved, so that #9's rear truck could be moved. Then everything (except the flatcars) were moved back.
* In the PM the diesel started, so with the hydraulic crane attached to the flatcar a train went north to get rail. A piece of the crane failed after 3 rails, meaning it could not lift any more rails. So the train returned, then put the flatcars back, and put Coach 3 and Car 103 back.
* Jason and others worked on #9's new frame, with Ed G machining supporting pieces.